Hydro turbine-governor model validation in pacific northwest
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This paper presents an approach for generator model validation based on the measurements taken at the point of interconnection. The approach is initially applied for The Dalles powerhouse, where the simulated and actual governor responses were found different. Governor tests and monitoring were performed and resulted in model revisions. The approach also resulted in improvements of John Day turbine-governor models. Grand Coulee governor response was validated and found adequate. Based on the project experience, a process for generator model validation is proposed.
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