한국형기동헬기 레이더고도계의 결함분석을 통한 신뢰성 향상에 관한 연구
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In this paper, it is introduced characteristics of FMCW-type Radar Altimeter for KUH, and its defects occurred during ground/flight test in initial product phase. In addition, it is also described "data/control flow model" based fault analysis results of S/W and processes of verifying improvement design through flight test as well as aircraft system integration test called MEP SIL. As a result of design improvement and verification, it is validated that settling the defects and improving not only safety but also capability of the KUH.
[1] 이상목,et al. 개정 헬리콥터 내추락성 설계기준 분석 , 2014 .
[2] 오현웅,et al. 수동형 자세제어 안정화 방식을 적용한 큐브위성의 열적 특성분석 , 2014 .