Past Performance analysis of HPOTP bearings

The past performance analysis conducted on three High Pressure Oxygen Turbopump (HPOTP) bearings from the Space Shuttle Main Engine is presented. Metallurgical analysis of failed bearing balls and races, and wear track and crack configuration analyses were carried out. In addition, one bearing was tested in laboratory at very high axial loads. The results showed that the cracks were surface initiated and propagated into subsurface locations at relatively small angles. Subsurface cracks were much more extensive than was appeared on the surface. The location of major cracks in the races corresponded to high radial loads rather than high axial loads. There was evidence to suggest that the inner races were heated to elevated temperatures. A failure scenario was developed based on the above findings. According to this scenario the HPOTP bearings are heated by a combination of high loads and high coefficient of friction (poor lubrication). Different methods of extending the HPOTP bearing life are also discussed. These include reduction of axial loads, improvements in bearing design, lubrication and cooling, and use of improved bearing materials.